Manufacturing Technology 2021, 21(1):56-64 | DOI: 10.21062/mft.2021.006
Improving Overall Equipment Effectiveness (OEE) of Extrusion Machine Using Lean Manufacturing Approach
- 1 Department of Industrial Engineering, An-Najah National University, Nablus, Palestine
- 2 Department of Manufacturing Science and Engineering, Budapest University of Technology and Economics, 1111 Budapest, Műegyetem rkp. 3, Hungary
- 3 Department of Manufacturing Science and Engineering, Budapest University of Technology and Economics, 1111 Budapest, Műegyetem rkp. 3, Hungary
Providing products with higher quality and lower prices is considered to be a competitive advantage for the industrial firms over competitors. This main challenge can be achieved by minimizing the overall production costs and operational time. Lean manufacturing provides many tools and techniques to iden-tify and eliminate wastes and to reduce costs in production systems. In this paper, single minute ex-change of die (SMED) technique is used as a lean manufacturing approach in a leading Palestinian aluminum profiles company. SMED was implemented through real experimental procedures applied to the extrusion line processes to investigate its effect on decreasing the setups time and improving the Overall Equipment Effectiveness (OEE) of the extrusion machine, in addition to introduce a guide for practitioners to improve the extrusion process dies exchange in similar industries. Overall, the successful implementation of SMED resulted in an increase of OEE by 3.26% as the consequence of the increase of machine availability by 4.86%.
Keywords: Overall Equipment Effectiveness (OEE), Single Minute Exchange of Die (SMED), Lean, Availability, Extrusion.
Grants and funding:
Palestinian aluminum and profiles’ company Ltd.
Received: September 30, 2020; Revised: January 5, 2021; Accepted: January 8, 2021; Prepublished online: February 10, 2021; Published: February 24, 2021 Show citation
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